Wyoming Interstate Notice 122510
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TSP/TSP Name: 30669048-WYOMING INTERSTATE CO. | Critical: Y |
Notice Type Desc (1): FORCE MAJEURE | Notice Type Desc (2): FORCE MAJEURE |
Notice Eff Date/Time: 07/16/2025 7:59:53AM | Notice End Date/Time: 07/17/2025 9:00:00am |
Post Date/Time: 7/16/2025 7:59:53 AM | Notice ID: 122510 |
Reqrd Rsp: 1 | Rsp Date: 07/16/2025 |
Notice Stat Desc: SUPERSEDE | Prior Notice: 122505 |
Subject: Cancellation Force Majeure Segment 428 |
Wyoming Interstate Company, L.L.C. July 16, 2025 Force Majeure Segment 428 - Cancelled |
Wyoming Interstate Company, L.L.C. (WIC) has completed the repairs at Creston Compressor Station on the Echo Springs Lateral (Segment 428), as such, WIC is lifting the Force Majeure declared in Notice No. 122505. The operational capacity will increase to 132,000 Dth/d in the TD1 direction effective Gas Day 16 July, 2025, Intraday 1, Cycle 3.
|
Pipeline
Scheduling Hotline or email CIGSched
|
Mike Burleson (719) 520-4523.
|
Marketing questions
Contact your Marketing Representative. |
Rich Aten, Manager – Pipeline Scheduling Transportation and Storage Services Kinder Morgan Rockies Pipelines (719) 667-7527 or (719) 648-5253
|
TSP/TSP Name: 30669048-WYOMING INTERSTATE CO. | Critical: Y |
Notice Type Desc (1): FORCE MAJEURE | Notice Type Desc (2): FORCE MAJEURE |
Notice Eff Date/Time: 07/16/2025 7:59:53AM | Notice End Date/Time: 07/17/2025 9:00:00am |
Post Date/Time: 7/16/2025 7:59:53 AM | Notice ID: 122510 |
Reqrd Rsp: 1 | Rsp Date: 07/16/2025 |
Notice Stat Desc: SUPERSEDE | Prior Notice: 122505 |
Subject: Cancellation Force Majeure Segment 428 |
Wyoming Interstate Company, L.L.C. July 16, 2025 Force Majeure Segment 428 - Cancelled |
Wyoming Interstate Company, L.L.C. (WIC) has completed the repairs at Creston Compressor Station on the Echo Springs Lateral (Segment 428), as such, WIC is lifting the Force Majeure declared in Notice No. 122505. The operational capacity will increase to 132,000 Dth/d in the TD1 direction effective Gas Day 16 July, 2025, Intraday 1, Cycle 3.
|
Pipeline
Scheduling Hotline or email CIGSched
|
Mike Burleson (719) 520-4523.
|
Marketing questions
Contact your Marketing Representative. |
Rich Aten, Manager – Pipeline Scheduling Transportation and Storage Services Kinder Morgan Rockies Pipelines (719) 667-7527 or (719) 648-5253
|